Larkin Engineering of Tuam, Galway were recently awarded for its green initiatives in the national ‘How Green is Your Business Competition’ held by the Dublin Chamber of Commerce with special guest, Dragon’s Den Judge, Bobby Kerr.
Noel Larkin, MD Larkin Engineering, and Bobby Kerr
“Larkin Engineering Street Products” is a line of products manufactured by the Tuam based company and is supported by the Environmental Protection Agency (EPA), programmes – the Cleaner Greener Production Programme (CGPP) and the National Waste Prevention Programme and a local company, SPeco Environmental Health and Safety Consultants, based in Galway. Under (CGPP) a number of environmental initiatives were investigated such as energy, waste and water minimisation, eco design and manufacturing efficiency.
Laura Burke, EPA Director said:
“Through the Cleaner Greener Production Programme, the EPA is assisting Irish enterprises to improve their environmental performance. Businesses like Larkin that participated in the EPA’s Cleaner Greener Production Programme have shown how achieving resource efficiency brings big economic opportunities. EPA study showed almost €1.6m per annum worth of savings for Cleaner Greener Production Programme companies from a one off investment by the EPA of €1m. The EPA is delighted to assist companies such as Larkin to grow in both an economic and environmentally-sustainable way.”
Through the ‘How Green is Your Business Competition’, Larkin Engineering demonstrated how Eco-design brought about new ideas. One such example involved the manufacture of a new bin using 38% less material. The company also started a take back system to refurbish existing bins rather than asking customers to purchase a new bin.
Below are some of the green efficiencies achieved by Larkin:
Eco-design
- Saved 38 % of the raw material previously being used on each 100 litre jumbo bin;
- Product take back and refurbishment: local authorities demonstrated that 3.5 bins could be refurbished for the same amount of energy as it would take to manufacture one new bin;
Energy
- Electricity usage was reduced by 9000 kWh per month in 2011 compared to 2010;
- Significant savings were achieved in energy spend per new bin;
Waste
- Over 40% reduction in the amount of metal being sent for recycling from production since 2008 due to improved material utilisation.
- 19% improvement in production efficiency due to improved layouts and work practices.
Water
- Rain water harvesting allowed the manufacturing plant to become self sustainable.



